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authorHans de Goede <hdegoede@redhat.com>2022-02-28 23:39:50 -0800
committerGreg Kroah-Hartman <gregkh@linuxfoundation.org>2022-03-08 19:01:58 +0100
commit674caa2728b25d556dd58b9794fa4964edd16918 (patch)
treeffe1b19de7472bc4d2bb74142967050ac6be5b56 /drivers
parent247c7fe81ef0b743edf124e2cea985ac883cd265 (diff)
Input: elan_i2c - fix regulator enable count imbalance after suspend/resume
commit 04b7762e37c95d9b965d16bb0e18dbd1fa2e2861 upstream. Before these changes elan_suspend() would only disable the regulator when device_may_wakeup() returns false; whereas elan_resume() would unconditionally enable it, leading to an enable count imbalance when device_may_wakeup() returns true. This triggers the "WARN_ON(regulator->enable_count)" in regulator_put() when the elan_i2c driver gets unbound, this happens e.g. with the hot-plugable dock with Elan I2C touchpad for the Asus TF103C 2-in-1. Fix this by making the regulator_enable() call also be conditional on device_may_wakeup() returning false. Signed-off-by: Hans de Goede <hdegoede@redhat.com> Link: https://lore.kernel.org/r/20220131135436.29638-2-hdegoede@redhat.com Signed-off-by: Dmitry Torokhov <dmitry.torokhov@gmail.com> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Diffstat (limited to 'drivers')
-rw-r--r--drivers/input/mouse/elan_i2c_core.c14
1 files changed, 7 insertions, 7 deletions
diff --git a/drivers/input/mouse/elan_i2c_core.c b/drivers/input/mouse/elan_i2c_core.c
index b9d124a02e44..3c7281248432 100644
--- a/drivers/input/mouse/elan_i2c_core.c
+++ b/drivers/input/mouse/elan_i2c_core.c
@@ -1195,17 +1195,17 @@ static int __maybe_unused elan_resume(struct device *dev)
struct elan_tp_data *data = i2c_get_clientdata(client);
int error;
- if (device_may_wakeup(dev) && data->irq_wake) {
+ if (!device_may_wakeup(dev)) {
+ error = regulator_enable(data->vcc);
+ if (error) {
+ dev_err(dev, "error %d enabling regulator\n", error);
+ goto err;
+ }
+ } else if (data->irq_wake) {
disable_irq_wake(client->irq);
data->irq_wake = false;
}
- error = regulator_enable(data->vcc);
- if (error) {
- dev_err(dev, "error %d enabling regulator\n", error);
- goto err;
- }
-
error = elan_set_power(data, true);
if (error) {
dev_err(dev, "power up when resuming failed: %d\n", error);